ap-3-11.dvi Acta Polytechnica Vol. 51 No. 3/2011 3D Modelling of a Tunnel Re-excavation in Soft Ground M. Hilar Abstract The construction of the shallow tunnel at Brezno started using the Pre-Vault Method. The tunnel excavation, in complicated geological conditions, led to many difficulties which finally resulted in a collapse, when a significant part of the temporary tunnel lining collapsed. Various options for re-excavating the tunnel were evaluated prior to further construction. Finally a decision was made to separate the collapsed area into sections 9 m in length using 16 m-wide, transversally oriented pile walls, to improve the stability of the collapsed ground. The walls were constructed from the surface prior to excavation. It was also decided to re-excavate a collapsed area using the SprayedConcrete Lining (SCL) method. Due to problematic soft ground conditions, which had been made even worse by the collapse, some additional support measures had to be considered prior to re-excavation (ground improvement, micropile umbrellas embedded into the pile walls, etc.) This paper describes numerical modelling of the tunnel re-excavation through the collapsed area. Initial calculations of the tunnel re-excavation were made using a 2D finite element method. Subsequently, further calculations to evaluate the rock mass behaviour in the collapsed area were provided in 3D. The 2D calculations were used to provide sensitivity studies, while 3D modelling was mainly used for evaluating the tunnel face stability (impact of the pile walls, impact of ground improvement) together with other factors (length of advances, moment of the temporary invert closure, etc.) The results of the modelling were compared with the monitoring results. The paper also briefly describes the construction experience (technical problems, performance of various support measures, etc.) The excavation and the primary lining construction were completed in 2006, and the tunnel was opened for traffic in April 2007. Keywords: tunnel, clay, soft ground tunnelling, sprayed concrete, New Austrian Tunnelling Method, NATM, Sprayed Concrete Lining, SCL, numerical modelling. History The construction of theBrezno tunnel, with overbur- den up to 30 m, started in 2000 using the Pre-Vault Method (Perforex) [1]. The Pre-Vault Method prin- ciple is such that a 20 cm-wide slit (for the Brezno tunnel) is cut along the upper and side parts of a pre- defined tunnel circumference. Step by step, simulta- neously with cutting the prescribed number of seg- ments in a prescribed sequence, the slit is filled with sprayed concrete. The hardened concrete forms a protective pre-vault reaching ahead of the rock exca- vation. The pre-vault has a truncated conical shape. This shape allows overlapping of the individual pre- vaults. The length of the chain saw determines the length of the pre-vault, which was 5 m in the case of the Brezno tunnel. The pre-vault can overlap the preceding prevault from 2.5 to 0.5m (the excavation advance length is selected according to the geological conditions that are encountered, from 2.5 to 4.5 m). Full-face excavation then takes place under protec- tion from the pre-prepared primary lining. The tunnel excavationwaspredominantly inplas- tic clays and claystones, and the maximum thickness of the quaternary deposits (gravels and sands) was about 6 m. The area was also affected by previous undocumented mining activities. The very compli- cated geological conditions caused many difficulties, resulting in a significant collapse in 2003. The col- lapse occurredwhen about 860m of the primary lin- ing of the tunnel had been completed. About 77 m of primary lining was destroyed (chain effect of pre- vaults) and a further 44 m of the tunnel was filled with collapsed material. Excavation ceased for sev- eral months directly after the collapse. Proposed tunnel recovery A decision was made to separate the collapsed area into 9m-long sections using 16m-wide tranverse pile walls constructed from the surface. The walls were formed from piles 1.18 m in diameter, and the walls reached 3 m below the tunnel profile. The collapsed tunnel was separated into 7 sections in the longitu- dinal direction. A shaft had to be constructed in the area of a buried Perforex machine (Figure 1). The Sprayed Concrete Lining (SCL) method was used for re-excavating the collapsed area. The pri- mary lining was designed as sprayed concrete, rein- forced by lattice girders and amesh. The tunnel face had to be excavated in several stages. The proposed excavationmethodhad tobeproperly statically eval- uated prior to application, and all support measures had to be optimised. 25 Acta Polytechnica Vol. 51 No. 3/2011 Fig. 1: Longitudinal cross-section, including separation of the collapsed area using pile walls Table 1: Input geotechnical parameters (the abbreviations of the layers correspond with Figure 2) Geotechnical unit Input parameters γ (kN/m3) c (kPa) φ (◦) EDEF (MPa) ν Quaternary deposits QD 19.2 11.5 18 17 0.30 Strongly weathered claystone SWC 19.2 11.0 10 19 0.40 Collapsed material CM 19.2 11.0 8 19 0.40 Weathered claystone WC 19.5 17.0 19 19 0.40 Claystone A CA 19.5 36.0 19 32 0.40 Claystone B CB 19.5 40.0 20 35 0.38 Claystone C CC 19.5 45.0 25 50 0.38 Coal seam CS 19.5 30.0 25 60 0.30 Fig. 2: 2D model finite element mesh (the abbreviations of the layers correspond with Table 1) The calculations were generated using the finite element method (FEM). Due to the complexity of the problem, ordinary 2D calculations were supple- mented by 3D calculations to verify some 3D effects (e.g. impact of tunnel separation by pile walls). Original calculations The initial static calculations for designing the pri- mary lining and the excavation sequence were gener- ated using 2DFEM(plane strainmodel) [2], and the rock mass was modelled using a linear elasto-plastic Mohr-Coulomb model (Figure 2). RIB software was used for the calculations [4]. The primary tunnel lin- ing was evaluated using interaction curves produced by FINE software [5]. The input parameters were derived from a supplementary site investigation con- ducted after the collapse. The initial input param- eters for each geotechnical unit are summarised in Table 1. The value used for the coefficient of the lateral pressure at rest was 0.8. The input parame- 26 Acta Polytechnica Vol. 51 No. 3/2011 ters were derived from a supplementary site investi- gation carried out after the collapse. The collapsed ground was quite heterogeneous (a mixture of cohe- sive and non-cohesive soils), and the selected mean values were rather conservative. The static calculations that were generatedmod- elled the excavation and support installation in sev- eral stages (top heading excavation, top heading lin- ing, benchexcavation,bench lining, invert excavation and invert lining closure), and the model included two types of sprayed concrete — three-day-old green sprayed concrete, and sprayed concrete with its final parameters. The lining thicknesswas35 cm. The top heading liningwas expected to be regularly closed by a temporary invert, which is a crucial measure for achieving equilibrium in geological conditions of this type. Geometry also plays a very important role in minimizing the bending moments (smaller eccentric- ity) in the lining. The lining geometrywas optimised in this way. The calculated maximal axial forces were in the range 1500 kN to 2450 kN, depending on the stage of excavation. The calculations confirmed that the maximum deformations of the primary lining should not exceed 50 mm, and monitoring during construc- tion generally confirmed these expectations. The shape of the temporary top heading invert was de- signed as a compromise between the optimum static profile and the space requirement for the machinery. The shape of the permanent invert was more appro- priate from the static view, as no compromises were required. The tunnel lining evaluation confirmed that its capacity was sufficient. Verification calculations 3D calculationswere generated using Plaxis 3DTun- nel software [6]. The major aim of this modelling was to evaluate the impact of the pile walls on the excavation and the lining. The model was prepared for analysing the conditions input into the 2D calcu- lations (location of geotechnical units, input param- eters, tunnel lining, etc.) The3Dmodelwas127m inheight, 90m inwidth, and 97m in length (Figure 3). The model comprised half of the tunnel, and used symmetry. First, the top heading constructionwasmodelled (Figure 4) in sev- eral steps to simulate top heading excavation. Each advancewasmodelled in two phases (excavation and tunnel lining application). Second, the bench and invert construction was modelled in several steps (Figure 5). Again, each ad- vance was modelled in two phases (excavation and tunnel lining application). One model was generated with pile walls (Figure 6); the second was generated without them. Fig. 3: 3D model finite element mesh (the geotechnical layers and parameters correspond with the 2D model) Fig. 4: Modelling of the top heading construction Fig. 5: Modelling of the bench and invert construction 27 Acta Polytechnica Vol. 51 No. 3/2011 Fig. 6: Details of the 3D model with pile walls Fig. 7: Top heading tunnel lining deformations (impact of pile walls) Impact of pile walls: The model included pile walls spaced at 9 m, with a thickness of 1 m (Fi- gure 6). The pile walls were modelled as a linear- elastic material, and they were separated into two parts to simulate the real structure (see Figure 6): a. Lower part (in the tunnel area) filled with con- crete with the properties: E =25 GPa, ν =0.2 b. Upper part (above the tunnel) filled by suspen- sion with the properties: E =10 GPa, ν =0.2 Two calculations were generated: with walls and without walls. The results showed the stiffening ef- fect of pile walls. The construction of the pile walls means a reduction in deformations (Figure 7) and bendingmoments of about 50%. The differences be- tween the 2D results and the 3D results (seeTable 2) were caused by the original estimation of the relax- ation. The choice of low relaxation (i.e. a fast ring closure assumption) in the 2D calculations was de- termined mainly by taking a conservative approach to the primary lining analysis (to get higher axial forces). Impact of bench and invert excavation: A further purpose of the 3D calculations was to evalu- ate the effect of bench and invert excavation on the 28 Acta Polytechnica Vol. 51 No. 3/2011 top heading lining performance (i.e. when the tunnel invert should be closed). The invert was modelled to be closedafter 2m(Figure8), 4m, and8madvances. The calculations showed that the values of the inter- nal forces in the top heading lining are not a signifi- cant problem. A more significant problem would be the deformations, which would double in the case of 8 m advances. The next problem was the forces in the longitudinal direction and the shear forces in the lining close to the walls (Figure 9). Thus, a max- imum advance of 4 m was recommended for bench and invert excavation. Fig. 8: Bench and invert constructionmodellingwith 2m advances Fig. 9: Concentration of shear forces in the tunnel lining on the interface of the pile walls and the ground Topheading face stability: Calculationsof the top heading face stability were also generated. The bench and invert excavationwas expected to be sepa- ratedat leastbyonepilewall tohaveaminimal effect on the stability of the top heading face. Again the calculation was performed in several stages to sim- ulate the tunnel construction procedure (installation of pilewalls, consequently several excavationsand in- stallations of lining). The tunnel face stability was calculated when the tunnel face was 2 m behind the pilewall and1mof the excavationwasnot supported by the tunnel lining. The safety factorwas calculated using the phi-c reduction procedure (option available in Plaxis for computing safety factors). In the phi-c reduction approach, the strength parameters tan φ and c of the ground were successively reduced until failure occurs. The resulting safety factor is the ratio of the initial and final shear parameters. The calculations showed a safety factor of 1.1, which indicated problems in the top heading face stability. However, the calculation that was gener- ated did not include the designed support measures (supportwedge,micropile umbrellas and jet grouting columns, further sequencing of the face, etc.) The results showed a favourable effect of pile walls in lim- iting the propagation of the deformations that were generated (Figure 10). Fig. 10: Propagation of the topheading face deformations Construction experience There was significant anxiety about the ground be- haviour prior to the start of excavation, as the area had been significantly disrupted by the previous col- lapse (the area in and above the tunnel profile). Coreswere thereforedrilled fromthe tunnel faceprior to excavation of each section between the pile walls, and a decision was made on ground improvement and supportmeasuresbasedon the results of drilling. In chamber 1 (see Figure 1), horizontal jet grouting columns were installed into the face to increase the face stability. This measure was also used in cham- ber 3 (see Figure 1). The tunnel profile was regularly protected bymi- cropile umbrellas (Figure 11); the micropiles were embedded into the pile walls on both ends. Some attempts were made to embed the micropiles into 29 Acta Polytechnica Vol. 51 No. 3/2011 Fig. 11: Tunnel construction under micropile umbrellas the horizontal jet grouting columns (to increase their stiffness), but like the jet grouting columns drilled into the face, this approach was finished after the third section. All excavations were done with 1 m advances. The excavatedprofilewas supported bywiremeshes, lattice girders and sprayed concrete. The face sta- bility was regularly increased by a support wedge (ground left in the centre of the excavated profile). In addition, a flash coat of sprayed concrete (sev- eral centimetres)was immediately appliedonthe face and tunnel perimeter after the excavation. The top heading facewas sometimes excavatedand sprayed in several steps (in cases of local instability). All these measures helped significantly to increase the tunnel face stability, and the calculated low tunnel face sta- bility was confirmed during excavation by several lo- cal failures. In addition, the temporary top heading invert was closed regularly. Originally it was closed in 2 m or 3 m steps, but later these sections were extended to 4 m. Bench and invert excavation was carried out more than 9 m behind the top heading face (the length of one chamber). The excavation started at the end of February 2006 and was com- pleted without major problems at the beginning of August 2006. Results of monitoring The ground deformations were recorded by ordinary geotechnical monitoring. The sprayed concrete lin- ing was monitored by convergence monitoring, with threepoints on the topheadingand twopoints on the bottom. The convergence cross-sectionswere located in the centre of all pile walls and also between the pile walls (generally one or two intermediate moni- toring profiles between two pile walls). The surface settlement wasmonitored on the top of all pile walls; some intermediatepoints at ground level between the walls were also monitored. The maximum surface settlement monitored above the tunnel was 28 mm (area above the cham- ber 2). 2D modelling predicted surface settlement of 40 mm, and 3D modelling with pile walls predicted 20 mm. All convergences generally remained below 40mm, but themonitoring results showed significant scatter of the tunnel lining deformations (Table 2), mainlydue to theverydifficult heterogeneousground conditions. In chamber 2, vault settlement of 93mm was monitored. This high deformation was caused by local problems (tunnel lining cracking), which did not affect the overall stability of the tunnel. 2Dmod- elling predicted vault settlement of 50mm, while 3D modelling with pile walls predicted vault settlement of 25 mm. The results are compared with the moni- toring results in Table 2. Naturally, even 3Dmodelling could not reflect all aspects of the excavation. When the modelling re- sults are compared with the actually measured de- formation values, some differences become obvious, but they are not too great in this particular case. The differences are mainly caused by factors which could not be properly included in the models (het- erogeneousground, timing andquality of the support measures, quality of the grouting, etc.) Conclusion The Brezno tunnel had to be excavated in very com- plicated geological conditions. These ground condi- tions were significantly worsened by the collapse of a long section of the tunnel lining. The design of the excavation procedure and appropriate support mea- sures for re-excavation of the collapsed tunnel was not a straightforward task. Static calculations of the tunnel re-excavation were provided using the 2D fi- nite element method (RIB software). Further calcu- lations for evaluating the rockmass behaviour in the collapsed area were provided using Plaxis FEM soft- ware. 2Dcalculationswereused toprovidesensitivity studies [3], and 3D modelling assisted the evaluation of the tunnel face stability (impact of the pile walls, ground improvement, etc.) The results of the mod- elling were compared with the monitoring results. The paper also briefly describes the construction ex- perience (technical problems, performance of various support measures, etc.) 2D and 3D modelling were used to evaluate the ground and tunnel behaviour prior to re-excavation. The modelling provided very useful information prior to the start of construction. It led to optimisa- tion of the tunnel shapeand the excavation sequence. It indicated tunnel face stability problems,whichhad to be improved by various measures. It also showed quite well some anticipated problems which subse- quently appeared during the excavation (low stabil- ity of the excavation face, concentration of stress be- 30 Acta Polytechnica Vol. 51 No. 3/2011 Table 2: Comparison of monitored and calculated tunnel lining crown settlement Tunnel chainage (m) Monitoring (mm) 2D Model (mm) 3D Model (mm) 2004 5 50 25 2007 19 50 25 2012 21 50 25 2019 20 50 22 2025 20 50 25 2027 27 50 25 2031 33 50 22 2034 37 50 25 2036 50 50 25 2040 93 50 22 2043 38 50 25 2048 39 50 22 2052 40 50 25 2057 40 50 22 2061 40 50 25 2066 31 50 22 2070 24 50 25 2075 26 50 22 2079 11 50 25 2081 17 50 24 tween the unclosed and closed linings, the positive influence of the temporary invert and dividing pile walls, etc.) Regarding the excavation itself, a flexible ap- proach to the construction work on the part of the contractor was essential. In some cases, it was nec- essary to respond to the properties and behaviour of the ground in a very flexible manner; it was impos- sible to optimise all aspects of the excavation in the planning phase. The excavation procedure was rea- sonably well optimised during construction, so the collapse recoverywas completed without any further significant difficulties. The Brezno tunnel construc- tion was successfully completed, and the tunnel was opened for traffic in April 2007. Acknowledgement Financial support from research grant TACR TA01011816 is gratefully acknowledged. References [1] Hilar, M., Heřt, J., Smida, M.: Soft Ground Ex- cavationof theBřeznoTunnel.Proceedings of the World Tunnelling Congress, Agra, 2008. [2] Hilar, M., John, V.: Recovery of a collapsed sec- tion of theBrezno tunnel.Tunel, Vol.16, 3/2007. [3] Barták,J.,Hilar,M., Pruška,J.: NumericalMod- elling of the Underground Structures. Acta Poly- technica. Vol. 42, No. 1/2002. [4] RIB — software for civil engineers. http://www.rib.cz [5] FINE — civil engineering software. http://www.fine.cz [6] Plaxis — software for geotechnical engineers. http://www.plaxis.nl doc. Ing. MatoušHilar, MSc., PhD., CEng.,MICE Phone: +420 604 862 686 E-mail: hilar@d2-consult.cz D2 Consult Prague, s.r.o. Zelený pruh 95/97 (KUTA) 140 00 Praha 4, Czech Republic Department of Geotechnics Faculty of Civil Engineering Czech Technical University in Prague Thákurova 7, 166 29 Praha 6, Czech Republic 31